Slow Car Fast
THE MG
September 7, 2010 - Janel and I have realized that the interior of the car is going to need some attention.
We bought this particular car because it was black with a tan interior, and it looked great. Of course, then it turned out to have a bad paint job and the interior was just spray painted. But we still got a good rust-free chassis!
Of course, if we're going to refresh the interior we have to deal with matching the paint or replace it all. The latter is tempting but we have the problem of the headliner. I do not want to replace it - and it actually looks pretty good.
Looking at various color samples online, it appears the (unpainted) seats are "biscuit" and they do match the rest of the interior. Unfortunately, Moss Motors doesn't sell this color for the GT, only the convertible. I found a shop in the UK that offers a full biscuit interior for the GT but I wanted a color sample to be sure. And here's what showed up in the mail today!
The good news is that I was right. The seats are biscuit and match the sample perfectly. The complete interior does include new seat coverings, but this way we know everything will match. Yay! A big thumbs up for Chase MG. I'll put in an order for the parts soon. It actually quite affordable, a full interior for less than the price of two seats from Moss.
entry 391 - tags: interior
September 7, 2010 - The new brake master cylinder is here.
I did some calculations a while back on brake master sizes, and the ideal (to match the Miata) ended up being 15/16". My plan to use the Miata booster fell through due to a critical lack of space. Well, I have the choice of the old 7/8" setup from the MG or a 1" Wilwood caliper. Since almost everyone prefers a hard pedal with a bit more effort to a softer one, I've decided to go with the Wilwood setup. This also means I don't have to mess around with British flares! I'm not going to bother with the brake plumbing yet, but since the master arrived I just had to bolt it in.
I also bled the clutch hydraulics, so I should theoretically have a functioning clutch. I don't have any way to tell for sure yet - I'll wait until Janel is around, then see if I can spin the driveshaft by hand when the clutch is depressed. Oh boy, I sure hope so. It feels good anyhow.
The power steering lines are also fully hooked up now. By this point, all the fluids in the car (other than the brakes) should be contained. So it's back to wiring...
entry 392 - tags: clutch, brakes, steering
September 9, 2010 - Power!
With a few spare minutes in the garage and a freshly connected main relay, I hooked up the battery to the car for the first time. First, of course, I had to come up with a good grounding point. Hopefully I did.
When I connected the battery, nothing happened. That's good.
Then I flipped on the main circuit breaker. Nothing happened. That's good.
Then I turned on the ignition and saw a light come on inside the dash. Must be the alternator light. I also heard the main relay click over and the fuse panel for switched power came alive. That's good!
No sparks, no shorts, no nasty smells. All the smoke stayed inside the wires. This may not seem like a big step, but now that I know I have a smoke-tight electrical system it'll be a lot easier to trace wires and determine that everything is hooked up correctly.
Woohoo!
entry 393 - tags: wiring, smoke, electrical
September 13, 2010 - I was at a track day this past weekend, exercising the Targa Miata.
So no work done on the MG. And I'm going to Oklahoma for a track day this upcoming weekend, so no work will be done this week either. But I did take 5 minutes to do a quick check of the MG's clutch. Janel was involved in the driver's seat while I crawled under the car to slide the driveshaft into the end of the transmission. Then I crawled back out, jacked up the rear axle a bit for more clearance, and crawled back under to slide the driveshaft in place.
Poor Janel had to follow instructions like "put it in gear. Okay, now put it in neutral. Now put it in gear and press the clutch down". Meanwhile, I was trying to turn the driveshaft. Good news - with the car in gear and the clutch engaged, I could not spin the shaft. But with the clutch pedal down, it would spin freely. This means the clutch is disengaging fully. Janel did not seem as excited as I was.
entry 394 - tags: clutch
September 30, 2010 - Wow, three consecutive weekends of track days followed by a weekend of off-roading in the Colorado mountains.
Followed by a few days of being seriously under the weather. Lots of fun with cars, but no time for the MG. I'll be back on it this weekend, though. Various bits and pieces required to piece the intake together have been trickling in. It's going to be tight. Of course.
entry 395 - tags: intake
October 5, 2010 - Trying to pick up from where I'd been, a month later, is a challenge.
Especially with wiring. But I've sorted out what I was doing and I'm starting to make forward progress again. Nothing big or exciting, just careful connection and testing of one circuit at a time.
entry 396 - tags: wiring
October 6, 2010 - Woohoo!
This might not look like a whole lot, but it means the electrical system is live and I can talk to the engine computer. All the sensors that could be expected to have readings with the engine off have readings, and they're all accurate. The throttle is wedged slightly open in case you're wondering about that 11.8% reading on the TPS.
Once again, no smoke was released. This is all going well.
entry 397 - tags: wiring
October 6, 2010 - Time for a good day of work.
I have a goal! First, I need to get the exhaust system assembled. I figured out good O2 sensor locations, drilled the pipes and welded in bungs for the two sensors. Easy enough. I also added a new hanger at the back on the right muffler to match one that was already in place on the left.
entry 398 - tags: exhaust
October 6, 2010 - All the parts have arrived for the intake system, but I'm still trying to decide exactly how to plumb it.
It's hard to get a 4" tube in between my engine and radiator! So, for the time being, I simply laid the filter on the fender for testing.
entry 399 - tags: intake
October 6, 2010 - My clever header design does cause problems with the spark plug wires.
So I dragged out a set of wires from the old Cadillac and pressed two of them into service. It's not pretty, but it'll do the job.
What job? I'm aiming for the first start on the car. It's close, really close. So most of the day was spent doing a lot of the little jobs that hadn't been done before.
entry 400 - tags: plug wires
October 6, 2010 - The last step before trying to start the car was to put some fuel in the tank and pressurize the system.
That didn't work! Well, it did, but not completely. The stock MG fuel system uses a couple of flared fittings that, typically for the British, are probably only found on Spitfires and MGs. One of them's on the fuel tank itself. So in order to plumb everything together, I retained one of the original fuel hoses in the return line. Bad idea. As soon as the system was up to pressure and excess fuel started to feed back to the tank, this thing started leaking like a garden hose. The inner rubber hose must be cracked in at least 10 places.
So I pulled the hose out and managed to piece together a replacement using one of the end fittings. After a bit of fiddling around, the fuel system was happy and full of pressure.
entry 401 - tags: fuel
October 6, 2010 - So?
Did it start? Well, no. It cranks happily and I did get it to cough really briefly, but overall it's just not exciting. Here's where the OBD-II scanner comes in handy. I can see that all the various sensors are reading properly - there's even measured airflow going through the intake on cranking - but the engine RPM is stuck at 0. If the computer doesn't think the engine is spinning, it's not going to try to fire the injectors or spark the plugs.
I checked the wiring for the cam angle sensor and the crank angle sensor. It's good in both cases. When Janel's home tomorrow, I'll check to make sure I'm getting spark. But that 0 RPM reading kinda tells me what I'm looking for first...
entry 402 - tags: start, wiring
October 6, 2010 - I posted a question about the no-start behavior of the MG on LS1tech.com, and got an answer almost immediately.
I need to disable the VATS system. That's an anti-theft setup that uses a resistor in the key. Since I'm not using the Camaro ignition switch or key, it needs to be bypassed or turned off.
A tuning program like HP Tuners can be used for the latter, and we have a copy at work. I also need to do a few other things such as turn off the EGR and the rear O2 sensors. HP Tuners is expensive - but luckily, Flyin' Miata has a copy. I'll have to pay to "mate" it with my computer, that that's fairly inexpensive relative to the cost of the program.
Will this fix it? Let's find out!
entry 403 - tags: start, VATS, HPtuner
October 7, 2010 - I borrowed a laptop with HPTuners software from work.
As soon as I got home, I hooked up the laptop, fired up the HPTuners software and used it to turn off a number of vestigial appendages in the car's computer. VATS anti-theft: off. EGR: off. Air pump: off. Rear O2 sensors: off. Skip shift: off. A quick upload and voila. The car should be ready to start.
I should point out that this is pretty common software. Most shops that tune GM engines have a copy. I suspect my local machine shop would be able to do this for me. You can also send your engine computer off to have it done elsewhere - for example, Painless Wiring will reflash the computer with these sorts of changes for free if you buy one of their harnesses. The fact that I have access to the Flyin' Miata copy simply means it's more convenient for me than most people, that's all.
Another alternative would have been to build an inexpensive VATS bypass. The plans are pretty easily found online, or you can buy one pre-made. There are lots of ways to solve this problem. Since I also wanted to turn off a few other features, the reflash was the best option for me.
entry 404 - tags: HPTuners, PCM, ECU, VATS
October 7, 2010 - It's aliiiiiive!
After reprogramming the computer - which took about 5 minutes, using software I'd never seen before - I ran upstairs and told Janel I had a surprise for her. She didn't know how close the car was to starting. I jumped in the car and hit the key. It cranked for a few seconds, then a few seconds more. But it was trying. So I tried again and VAROOOOOOOOOM! Lots of noise, lots of revs, and a running engine.
I caught it all on video. It's a cinematic masterpiece, with expository dialogue, a build-up of tension and then a big climax followed by a happy denouement. In case you're wondering, I was talking to Janel who is standing at a safe distance behind the camera, taking refuge behind the Mini.
Watch it!

It wasn't completely successful. The first few times it didn't want to stay running more than a couple of seconds. It eventually settled down and kept running, but at a 2500 rpm idle. Since the main goal was to simply get it to work, I declared that enough. Even just a few seconds of running was enough to get the paint on the headers to bake in and release a nice cloud of smoke. I'll spend some more time cleaning up the wiring and hunting for vacuum leaks. Maybe this weekend I'll let it run for a bit longer to see if the engine speed will settle down as the computer re-learns this engine. The change in behavior from the first start to the fourth was notable.
First I need to blow the smoke out of the garage. Whew!
entry 405 - tags: first start, engine, video
October 12, 2010 - More progress.
A quick test with a smoke machine uncovered a vacuum port on the back of the intake manifold, underneath the MAP sensor. Almost impossible to see, and now capped. With that done, the idle quickly settled down under 1000 rpm and was continuing to improve when I shut things down. So it's looking as if the engine is a happy bunny.
I found an error in the wiring diagram I'm using. The engine computer is supposed to have a constant 12v feed to store all the various internal settings. According to the diagram, that feed was switched power so it only turned on with the key. Every time the computer loses power, it needs to relearn various settings such as the idle - so this would have been an annoying problem. Fixed now!
I'm working on related wiring now. The coolant gauge is hooked up, but the engine hasn't been hot enough to test it yet. I'm working on the tach now.
I also picked up all the pieces I need to complete the braking system. At least, I think I have all the pieces now. I'll start working on that soon, as it's the biggest step preventing me from actually driving the car. Ooooo!
entry 406 - tags: brakes, wiring, engine
October 13, 2010 - I'm all excited about working on the car right now.
But I'm very easily side-tracked. For example, I need to build the brake system. I had my head in the front wheel wells trying to figure out the best way to route the lines - it's hard to keep them away from the header - when I spotted the wiring for the front lights dangling. They'd been damaged at some point in the past and repaired poorly with solder. Well, it would be easier to patch them before I assemble the suspension, so I quickly hooked them back up with good connections. Then, of course, I wanted to see if they'd work and that led me to the steering column combo switch, which came from a Miata. So I ended up poring over Miata wiring diagrams and MG diagrams and trying to figure out how they each work so I can splice them together.
At the end of the night, I had functioning headlights but I hadn't energized the turn indicator circuits yet, and I'd temporarily run a switch in place of the headlight relay as I puzzled out the logic of both systems. Naturally, I'd made no progress on the brakes.
But it was fun, and I've turned the MG into a giant V8-powered flashlight.
entry 407 - tags: wiring, lights
October 19, 2010 - The wiring is moving right along.
It may not look any better than it did before, but the majority of the MG circuits are hooked up now, and the back half of the car is almost fully functional. Reverse lights, taillights, brake lights - all I need to do is make the flashers work, and that's just a matter of figuring out where in the harness the flasher unit was plugged in before! The main front/rear wiring harness has been relocated to run inside the car as there are hot exhaust pipes running back and forth underneath now, and the length is pretty much perfect. The wiring is really proving to be an easier job than it should be, in large part because the lengths of both the MG and GM harnesses have been bang on.
entry 408 - tags: wiring
October 19, 2010 - The intake is coming along.
It's a bit of an awkward thing, dropping from 4" to 3.5" (the diameter of the MAF) and then down to 3". I could probably keep it 3.5" from the MAF to the filter, but 1) I have a filter with a 3" inlet and 2) I have a box full of nice 3" piping and mandrel bends! Besides, the actual throttle body size is pretty much 3".
Tight packaging though. No surprise there.
entry 409 - tags: intake
October 26, 2010 - The completed intake.
All of the silicone pieces needed to be cut down as short as possible to allow the MAF to tuck into a spot beside the power steering reservoir, but it all fits. An S-shaped tube made of stainless steel exhaust mandrel bends joins the filter to the MAF, and also has a tab to support the intake. It's mounted to a rubber isolator, but I think the engine movement will be small enough that the silicone pieces will be able to take up the slack.
Sharp eyes will notice that the blue silicone has magically turned to black. This was due to clever use of electrical tape. It's not high-end, but it worked a treat!
entry 410 - tags: intake